http://SaturnianCosmology.Org/ mirrored file For complete access to all the files of this collection see http://SaturnianCosmology.org/search.php ========================================================== Space Shuttle Columbia disaster From Wikipedia, the free encyclopedia Jump to:navigation , search For further information about Columbia's mission and crew, see STS-107 . CNN International reports /Columbia/ disintegration. STS-107 mission patch STS-107 reentry The *Space Shuttle /Columbia/ disaster* occurred on February 1, 2003, when the Space Shuttle /Columbia/ disintegrated over Texas stretching from Trophy Club to Tyler and into parts of Louisiana during re-entry into the Earth's atmosphere , resulting in the death of all seven crew members, shortly before it was scheduled to conclude its 28th mission, STS-107 . The loss of /Columbia/ was a result of damage sustained during launch when a piece of foam insulation the size of a small briefcase broke off the Space Shuttle external tank (the main propellant tank) under the aerodynamic forces of launch. The debris struck the leading edge of the left wing, damaging the Shuttle's thermal protection system (TPS) , which protects it from heat generated with the atmosphere during re-entry. While /Columbia/ was still in orbit, some engineers suspected damage, but NASA managers limited the investigation, on the grounds that little could be done even if problems were found.^[1] NASA's original Shuttle design specifications stated that the external tank was not to shed foam or other debris; as such, strikes upon the Shuttle itself were safety issues that needed to be resolved before a launch was cleared. Launches were often given the go-ahead as engineers came to see the foam shedding and debris strikes as inevitable and unresolvable, with the rationale that they were either not a threat to safety, or an acceptable risk. The majority of Shuttle launches recorded such foam strikes and thermal tile scarring.^[2] During re-entry of STS-107, the damaged area allowed the hot gases to penetrate and destroy the internal wing structure,^[3] rapidly causing the in-flight breakup of the vehicle. A massive ground search in parts of Texas, Louisiana and Arkansas recovered crew remains and many vehicle fragments. Mission STS-107 was the 113th Space Shuttle launch. It was delayed 18 times over the two years from its original launch date of January 11, 2001, to its actual launch date of January 16, 2003. (It was preceded by STS-113 .) A launch delay due to cracks in the shuttle's propellant distribution system occurred one month before a July 19, 2002, launch date. The Columbia Accident Investigation Board (CAIB) determined that this delay had nothing to do with the catastrophic failure six months later. The Columbia Accident Investigation Board's recommendations addressed both technical and organizational issues. Space Shuttle flight operations were delayed for two years by the disaster, similar to the /Challenger/ disaster . Construction of the International Space Station was put on hold, and for 29 months the station relied entirely on the Russian Federal Space Agency for resupply until Shuttle flights resumed with STS-114 and 41 months for crew rotation until STS-121 . Contents [hide ] * 1 Crew * 2 Debris strike during launch * 3 Flight risk management * 4 Destruction during re-entry * 5 Presidential response * 6 Recovery of debris o 6.1 Onboard video * 7 Initial investigation * 8 Columbia Accident Investigation Board o 8.1 Possible emergency procedures * 9 Sociocultural aftermath o 9.1 Fears of terrorism o 9.2 Purple streak image o 9.3 Film hoax * 10 Memorials * 11 Impact on space programs * 12 See also * 13 References * 14 External links [edit ] Crew The crew of STS-107 . L to R: Brown , Husband , Clark , Chawla , Anderson , McCool , Ramon . * Commander: Rick D. Husband , a U.S. Air Force colonel and mechanical engineer , who piloted a previous shuttle during the first docking with the International Space Station (STS-96 ). * Pilot: William C. McCool , a U.S. Navy commander * Payload Commander: Michael P. Anderson , a U.S. Air Force lieutenant colonel and physicist who was in charge of the science mission. * Payload Specialist: Ilan Ramon , a colonel in the Israeli Air Force and the first Israeli astronaut. * Mission Specialist: Kalpana Chawla , an Indian-born aerospace engineer on her second space mission. * Mission Specialist: David M. Brown , a U.S. Navy captain trained as an aviator and flight surgeon . Brown worked on a number of scientific experiments. * Mission Specialist: Laurel Clark , a U.S. Navy captain and flight surgeon. Clark worked on a number of biological experiments. [edit ] Debris strike during launch /Columbia/ lifting off on its final mission. The light-colored triangle visible at the base of the strut near the nose of the orbiter is the Left Bipod Foam Ramp. Video Close-up of the Left Bipod Foam Ramp that broke off and damaged the Shuttle wing. Approximately 82 seconds after launch from Kennedy Space Center's LC-39-A, a suitcase-size piece of thermal insulation foam broke off the External Tank (ET), striking Columbia's left wing Reinforced Carbon-Carbon (RCC) panels. As demonstrated by ground experiments conducted by the Columbia Accident Investigation Board, this likely created a 6-to-10-inch (15 to 25 cm) diameter hole, allowing hot gases to enter the wing when Columbia later reentered the atmosphere. At the time of the foam strike, the orbiter was at an altitude of about 66,000 feet (20 km; 13 mi), traveling at Mach 2.46 (1,870 miles per hour or 840 m/s). The Left Bipod Foam Ramp is an approximately three-foot (one-meter) aerodynamic component made entirely of foam, as opposed to being a metal structure coated with foam. As such, the foam, not normally considered to be a structural material, is required to bear some aerodynamic loads. Because of these special requirements, the casting-in-place and curing of the ramps may be performed only by a senior technician.^[4] The shuttle's main fuel tank is covered in foam as an insulator, to avoid ice forming on it when full of liquid hydrogen and oxygen , which itself could damage the shuttle when shed during lift-off. The bipod ramp (having left and right sides) was originally designed to reduce aerodynamic stresses around the bipod attachment points at the external tank, but it was proven unnecessary in the wake of the accident and was removed from the external tank design for tanks flown after STS-107. (Another foam ramp along the liquid oxygen line was also later removed from the tank design to eliminate it as a foam debris source, after complex analysis and tests proved this change safe.) Bipod Ramp insulation had been observed falling off, in whole or in part, on many previous flights: STS-7 (1983), STS-27 (1988),^[5] STS-32 (1990), STS-50 (1992), plus subsequent flights (STS-52 and -62 ) showing partial losses. In STS-27's case, the damage was so severe that the spacecraft commander expected to die during reentry.^[5] In addition, Protuberance Air Load (PAL) ramp foam has also shed pieces, plus spot losses from large-area foams. At least one previous strike caused no serious damage. NASA management came to refer to this phenomenon as "foam shedding." As with the O-ring erosions that ultimately doomed the /Challenger/, NASA management became accustomed to these phenomena when no serious consequences resulted from these earlier episodes. This phenomenon was termed "normalization of deviance" by sociologist Diane Vaughan in her book on the /Challenger/ launch decision process .^[6] Video taken during lift-off of STS-107 was routinely reviewed two hours later and revealed nothing unusual. The following day, higher-resolution film that had been processed overnight revealed the foam debris striking the left wing, potentially damaging the thermal protection on the Space Shuttle. At the time, the exact location where the foam struck the wing could not be determined due to the low resolution of the tracking camera footage. [edit ] Flight risk management In a risk-management scenario similar to the /Challenger/ disaster, NASA management failed to recognize the relevance of engineering concerns for safety. Two examples were failures to honor engineer requests for imaging to inspect possible damage, and failure to respond to engineer requests about the status of astronaut inspection of the left wing. Engineering made three separate requests for Department of Defense (DOD) imaging of the shuttle in orbit to more precisely determine damage. While the images were not guaranteed to show the damage, the capability existed for imaging of sufficient resolution to provide meaningful examination. The CAIB recommended subsequent shuttle flights be imaged while in orbit using ground-based or space-based Department of Defense assets.^[7] NASA management did not honor the requests and in some cases intervened to stop the DOD from assisting.^[/citation needed /] NASA's chief thermal protection system (TPS) engineer was concerned about left wing TPS damage and asked NASA management whether an astronaut would visually inspect it. NASA managers never responded. Throughout the risk assessment process, senior NASA managers were influenced by their belief that nothing could be done even if damage was detected, hence this affected their stance on investigation urgency, thoroughness and possible contingency actions. They decided to conduct a parametric "what-if" scenario study more suited to determine risk probabilities of future events, instead of inspecting and assessing the actual damage. The investigation report in particular singled out NASA manager Linda Ham for exhibiting this attitude.^[8] Much of the risk assessment hinged on damage predictions to the thermal protection system. These fall into two categories: damage to the silica tile on the wing lower surface, and damage to the reinforced carbon-carbon (RCC) leading-edge panels. (The TPS includes a third category of components, thermal insulating blankets, but damage predictions are not typically performed on them. Damage assessments on the thermal blankets can be performed after an anomaly has been observed, and this has been done, at least once after the Return to Flight following Columbia's loss.) Damage-prediction software was used to evaluate possible tile and RCC damage. The tool for predicting tile damage was known as "Crater", described by several NASA representatives in press briefings as not actually a software program but rather a statistical spreadsheet of observed past flight events and effects. The "Crater" tool predicted severe penetration of multiple tiles by the impact if it struck the TPS tile area, but NASA engineers downplayed this. The engineers believed that results showing that the model overstated damage from small projectiles meant that the same would be true of larger Spray-On Foam Insulation (SOFI) impacts. The program used to predict RCC damage was based on small ice impacts the size of cigarette butts, not larger SOFI impacts, as the ice impacts were the only recognized threats to RCC panels up to that point. Under 1 of 15 predicted SOFI impact paths, the software predicted an ice impact would completely penetrate the RCC panel. Engineers downplayed this, too, believing that impacts of the less dense SOFI material would result in less damage than ice impacts. In an e-mail exchange, NASA managers questioned whether the density of the SOFI could be used as justification for reducing predicted damage. Despite engineering concerns about the energy imparted by the SOFI material, NASA managers ultimately accepted the rationale to reduce predicted damage of the RCC panels from possible complete penetration to slight damage to the panel's thin coating.^[9] Ultimately the NASA Mission Management Team felt there was insufficient evidence to indicate that the strike was an unsafe situation, so they declared the debris strike a "turnaround" issue (not of highest importance) and denied the requests for the Department of Defense images. [edit ] Destruction during re-entry The following is a timeline of /Columbia's/ re-entry. The shuttle was scheduled to land at 9:16 a.m. EST. * /2:30 a.m. EST, Saturday, February 1, 2003/ – The Entry Flight Control Team began duty in the Mission Control Center . The Flight Control Team had not been working on any issues or problems related to the planned de-orbit and re-entry of Columbia. In particular, the team had indicated no concerns about the debris impact to the left wing during ascent, and treated the re-entry like any other. The team worked through the de-orbit preparation checklist and re-entry checklist procedures. Weather forecasters, with the help of pilots in the Shuttle Training Aircraft , evaluated landing-site weather conditions at the Kennedy Space Center. * /8:00/ – Mission Control Center Entry Flight Director LeRoy Cain polled the Mission Control room for a GO/NO-GO decision for the de-orbit burn. All weather observations and forecasts were within guidelines set by the flight rules, and all systems were normal. * /8:10/ – The Capsule Communicator (CAPCOM) notified the crew that they were GO for de-orbit burn. * /8:15:30 (EI-1719)/ – Commander Husband and Pilot McCool executed the de-orbit burn using Columbia’s two Orbital Maneuvering System engines. The Orbiter was upside down and tail-first over the Indian Ocean at an altitude of 175 miles (282 km) when the burn was executed. The de-orbit maneuver was performed on the 255th orbit, and the 2-minute, 38-second burn slowed the Orbiter from 17,500 miles per hour (7.8 km/s) to begin its re-entry into the atmosphere. During the de-orbit burn, the crew felt about 10% of the effects of gravity . There were no problems during the burn, after which Husband maneuvered Columbia into a right-side-up, forward-facing position, with the Orbiter's nose pitched up. * /8:44:09 (EI+000)/ – Entry Interface (EI), arbitrarily defined as the point at which the Orbiter enters the discernible atmosphere at 400,000 feet (120 km; 76 mi), occurred over the Pacific Ocean. As Columbia descended from outer space into the atmosphere, the heat produced by air molecules colliding with the Orbiter typically caused wing leading-edge temperatures to rise steadily, reaching an estimated 2,500 °F (1,370 °C) during the next six minutes. (As former Space Shuttle Program Manager Wayne Hale stated in a press briefing, the majority--about 90%--of this heating is the result of compression of the atmospheric gas caused by the orbiter's supersonic flight, rather than the result of friction.) * /8:48:39 (EI+270)/ – A sensor on the left wing leading edge spar showed strains higher than those seen on previous Columbia re-entries. This was recorded only on the Modular Auxiliary Data System, which is similar in concept to a flight data recorder , and was not telemetered to ground controllers or displayed to the crew. * /8:49:32 (EI+323)/ – Columbia executed a pre-planned roll to the right. Speed: Mach 24.5. Columbia began a banking turn to manage lift and therefore limit the Orbiter's rate of descent and heating. * /8:50:53 (EI+404)/ – Columbia entered a 10-minute period of peak heating, during which the thermal stresses were at their maximum. Speed: Mach 24.1; altitude: 243,000 feet (74 km; 46 mi). /Columbia/ at approximately 8:57. Debris is visible coming off from the left wing (bottom). * /8:52:00 (EI+471)/ – Columbia was approximately 300 miles (480 km) west of the California coastline. The wing leading-edge temperatures usually reached 2,650 °F (1,450 °C) at this point. * /8:53:26 (EI+557)/ – Columbia crossed the California coast west of Sacramento. Speed: Mach 23; altitude: 231,600 feet (70.6 km; 43.9 mi). /Columbia/ debris (in red, orange, and yellow) detected by National Weather Service radar over Texas and Louisiana . A makeshift memorial at the main entrance to the Lyndon B. Johnson Space Center in Houston, Texas The Orbiter's wing leading edge typically reached more than 2,800 °F (1,540 °C) at this point. * /8:53:46 (EI+597)/ – Signs of debris being shed were sighted by people out to watch. Speed: Mach 22.8; altitude: 230,200 feet (70.2 km; 43.6 mi). The superheated air surrounding the Orbiter suddenly brightened, causing a streak in the Orbiter's luminescent trail that was quite noticeable in the pre-dawn skies over the West Coast. Observers witnessed another four similar events during the following 23 seconds. Dialogue on some of the amateur footage indicates the observers were aware of the abnormality of what they were filming. * /8:54:24 (EI+613)/ – The Maintenance, Mechanical, and Crew Systems (MMACS) officer informed the Flight Director that four hydraulic sensors in the left wing were indicating "off-scale low." In Mission Control, re-entry had been proceeding normally up to this point. "Off-scale low" is a reading that falls below the minimum capability of the sensor, and it usually indicates that the sensor has failed (stopped functioning, due to internal or external factors), rather than that the quantity it measures is actually below the sensor's minimum response value. The Entry Team continued to discuss the failed indicators. * /8:54:25 (EI+614)/ – Columbia crossed from California into Nevada airspace. Speed: Mach 22.5; altitude: 227,400 feet (69.3 km; 43.1 mi). Witnesses observed a bright flash at this point and 18 similar events in the next four minutes. * /8:55:00 (EI+651)/ – Nearly 11 minutes after Columbia re-entered the atmosphere, wing leading-edge temperatures normally reached nearly 3,000 °F (1,650 °C). * /8:55:32 (EI+683)/ – Columbia crossed from Nevada into Utah. Speed: Mach 21.8; altitude: 223,400 feet (68.1 km; 42.3 mi). * /8:55:52 (EI+703)/ – Columbia crossed from Utah into Arizona. * /8:56:30 (EI+741)/ – Columbia initiated a roll reversal, turning from right to left over Arizona. * /8:56:45 (EI+756)/ – Columbia crossed from Arizona to New Mexico. Speed: Mach 20.9; altitude: 219,000 feet (67 km; 41 mi). * /8:57:24 (EI+795)/ – Columbia crossed just north of Albuquerque. * /8:58:00 (EI+831)/ – At this point, wing leading-edge temperatures typically decreased to 2,880 °F (1,580 °C). * /8:58:20 (EI+851)/ – Columbia crossed from New Mexico into Texas. Speed: Mach 19.5; altitude: 209,800 feet (63.9 km; 39.7 mi). At about this time, the Orbiter shed a Thermal Protection System tile, the most westerly piece of debris that has been recovered. Searchers found the tile in a field in Littlefield, Texas , just northwest of Lubbock. * /8:59:15 (EI+906)/ – MMACS informed the Flight Director that pressure readings had been lost on both left main landing-gear tires. The Flight Director then told the Capsule Communicator (CAPCOM) to let the crew know that Mission Control saw the messages and was evaluating the indications, and added that the Flight Control Team did not understand the crew's last transmission. * /8:59:32 (EI+923)/ – A broken response from the mission commander was recorded: "Roger, uh, bu - [cut off in mid-word] ..." It was the last communication from the crew and the last telemetry signal received in Mission Control. * /8:59:37 (EI+928)/ – Hydraulic pressure, which is required to move the flight control surfaces, was lost at approximately GMT 13:59:37. At that time, the Master Alarm would have sounded for the loss of hydraulics and the crew would have become aware of a serious problem.^[10] * /9:00:18 (EI+969)/ – Videos and eyewitness reports by observers on the ground in and near Dallas, Texas revealed that the Orbiter had disintegrated overhead, continuing to break up into more and smaller pieces, and leaving multiple contrails , as it continued eastward. In Mission Control, while the loss of signal was a cause for concern, there was no sign of any serious problem. Prior to orbiter breakup at GMT 14:00:18, the Columbia cabin pressure was nominal and the crew was capable of conscious actions.^[10] * /9:05/ – Residents of north central Texas, particularly near Tyler, reported a loud boom, a small concussion wave, smoke trails and debris in the clear skies above the counties east of Dallas. * /9:12:39 (EI+1710)/ – After hearing of reports of the shuttle being seen to break apart, the NASA flight director declared a contingency (events leading to loss of the vehicle) and alerted search and rescue teams in the debris area. He made a call to the Ground Controller : "GC; flight, GC; flight. Lock the doors." Two minutes later Mission Control put contingency procedures into effect. Nobody was permitted to enter or leave the room, and flight controllers had to preserve all the mission data for later investigation.^[11] [edit ] Presidential response Play sound George W Bush Columbia FINAL.ogg Bush's address on the /Columbia'/s destruction, February 1, 2003. At 14:04 EST (19:04 UTC), President George W. Bush addressed the United States: "This day has brought terrible news and great sadness to our country ... The /Columbia/ is lost; there are no survivors." Despite the disaster, the President assured Americans that the space program would continue: "The cause in which they died will continue. Our journey into space will go on."^[12] [edit ] Recovery of debris More than 2,000 debris fields, including human remains, were found in sparsely populated areas southeast of Dallas from Nacogdoches in East Texas , where a large amount of debris fell, to western Louisiana and the southwestern counties of Arkansas . Within the months following the tragedy the largest ever organized ground search took place.^[13] NASA issued warnings to the public that any debris could contain hazardous chemicals, that it should be left untouched, its location reported to local emergency services or government authorities, and that anyone in unauthorized possession of debris would be prosecuted. Because of the widespread area, volunteer amateur radio operators accompanied the search teams to provide communications support.^[14] A group of small (1 mm adult) /Caenorhabditis elegans / worms, living in petri dishes enclosed in aluminium canisters, survived re-entry and impact with the ground and were recovered weeks after the disaster.^[15] ^[16] The culture was verified as still alive on April 28, 2003.^[17] They were part of a Biological Research in canisters experiment designed to study the effect of weightlessness on physiology. Debris Search Pilot Jules F. Mier Jr. and Debris Search Aviation Specialist Charles Krenek died in a helicopter crash that injured three others while they were contributing to the ground search effort.^[18] Some Texas residents recovered some of the debris, ignoring the warnings, and attempted to sell it on the online auction site eBay , starting at $10,000. The auction was quickly removed, but auctions for Columbia merchandise such as programs, photographs and patches, went up dramatically in value immediately following the disaster, creating a surge of Columbia-related listings.^[19] A three-day amnesty offered for looted shuttle debris brought in hundreds of illegally recovered pieces.^[20] There were approximately 40,000 recovered pieces of debris that were never identified. The largest pieces recovered include the front landing gear^[21] , a window frame, and a large section of the nose cone.^[22] On May 9, 2008 it was reported that data from a disk drive on board Columbia survived the shuttle accident.^[23] The drive was used to store data from an experiment on the properties of shear thinning .^[24] Although part of the 340MB drive was damaged, the area that contained the data was unharmed and could be recovered. [edit ] Onboard video The glow of reentry as seen out the front windows One item recovered from the debris field was a videotape recording made by the astronauts during the start of re-entry. The video recording lasts for thirteen minutes and shows the flight crew astronauts conducting routine re-entry procedures and joking with each other, none of them giving any indication of a problem. The video shows the flight-deck crew putting on their gloves and passing the video camera around in order to take footage of plasma and flames visible outside the windows of the orbiter (a completely normal occurrence), and ends approximately four minutes prior to the start of the shuttle's disintegration. On normal flights, the recording would have continued through landing. According to the online introduction given by Scott Altman , the remainder of the tape was destroyed in the accident. ^[/citation needed /] [edit ] Initial investigation NASA Space Shuttle Program Manager Ron Dittemore reported that "The first indication was loss of temperature sensors and hydraulic systems on the left wing. They were followed seconds and minutes later by several other problems, including loss of tire pressure indications on the left main gear and then indications of excessive structural heating".^[25] Analysis of 31 seconds of telemetry data which had initially been filtered out because of data corruption within it showed the shuttle fighting to maintain its orientation, eventually using maximum thrust from its Reaction Control System jets. The investigation focused on the foam strike from the very beginning. Incidents of debris strikes from ice and foam causing damage during take-off were already well known, and had actually damaged orbiters, most noticeably during STS-45 , STS-27 , and STS-87 .^[26] Tile damage had also been traced to ablating insulating material from the cryogenic fuel tank in the past. The composition of the foam insulation had been changed in 1997 to exclude the use of freon , a chemical that is suspected to cause ozone depletion ; while NASA was exempted from legislation phasing out CFCs, the agency chose to change the foam nonetheless. This led to many accusations of environmental pressures leading to the foam strikes.^[/citation needed /] STS-107 used an older "lightweight tank" (a design that was succeeded by the "superlightweight tank", both being upgrades from the original space shuttle external tank) where the foam was sprayed on to the larger cylindrical surfaces using the newer freon-free foam. However, the bipod ramps were manufactured from BX-250 foam which was excluded from the EPA regulations and did use the original freon formula. The composition change did not contribute to the accident.^[27] In any case, the original formulation had shown frequent foam losses, as discussed earlier in this article. [edit ] /Columbia/ Accident Investigation Board Main article: Columbia Accident Investigation Board Grid on the floor of the Reusable Launch Vehicle Hangar where workers in the field bring in pieces of /Columbia'/s debris. The /Columbia/ Reconstruction Project Team attempted to reconstruct the bottom of the orbiter as part of the investigation into the accident. A mock-up of a space shuttle leading edge made with an RCC -panel taken from /Discovery/ . Simulation of known and possible conditions of the foam impact on /Columbia/ 's final launch showed brittle failure of RCC. Following protocols established after the loss of /Challenger /, an independent investigating board was created immediately following the accident. The Columbia Accident Investigation Board, or CAIB, consisted of expert military and civilian analysts who investigated the accident in great detail. /Columbia's/ flight data recorder was found near Hemphill, Texas on March 20, 2003. Unlike commercial jet aircraft, the space shuttles do not have flight data recorders intended for after-crash analysis. Rather the vehicle data is transmitted in real time to the ground via telemetry . However, since /Columbia/ was the first shuttle, it had a special flight data OEX (Orbiter EXperiments) recorder, designed to help engineers better understand vehicle performance during the first test flights. After the initial Shuttle test-flights were completed, the recorder was never removed from /Columbia/ and was still functioning on the crashed flight. It records many hundreds of different parameters and contained very extensive logs of structural and other data which allowed the CAIB to reconstruct many of the events during the process leading to breakup. Investigators could often use the loss of signals from sensors on the wing to track how the damage progressed. This was correlated with forensic debris analysis conducted at Lehigh University and other tests to obtain a final conclusion about the probable events. On July 7, 2003 foam impact tests were performed by Southwest Research Institute , which used a compressed air gun to fire a foam block of similar size and mass to that which struck /Columbia/ and at same estimated speed. To represent the leading edge of Columbia's left wing, RCC panels from /Enterprise / and from NASA stock, along with fiberglass mock-up panels, were mounted to a simulating structural metal frame. Over many days, tens of these blocks of foam were shot at the wing leading edge model at various angles, aimed at different specific RCC panels, most of which produced only cracks or surface damage to the RCC. In the final round of testing, a block fired at the side of an RCC panel created a hole 41 by 42.5 centimeters (16 by 16.7 in) in the protective RCC panel.^[28] The tests clearly demonstrated that a foam impact of the type /Columbia/ sustained could seriously breach the thermal protection system on the wing leading edge.^[29] On August 26, the CAIB issued its report on the accident. The report confirmed the immediate cause of the accident was a breach in the leading edge of the left wing, caused by insulating foam shed during launch. The report also delved deeply into the underlying organizational and cultural issues that led to the accident. The report was highly critical of NASA's decision-making and risk-assessment processes. It concluded the organizational structure and processes were sufficiently flawed and that compromise of safety was expected no matter who was in the key decision-making positions. An example was the position of Shuttle Program Manager, where one individual was responsible for achieving safe, timely launches and acceptable costs, which are often conflicting goals. The CAIB report found that NASA had accepted deviations from design criteria as normal when they happened on several flights and did not lead to mission-compromising consequences. One of those was the conflict between a design specification stating the thermal protection system was not designed to withstand significant impacts and the common occurrence of impact damage to it during flight. The board made recommendations for significant changes in processes and organizational culture. On December 30, 2008 NASA released a further report, entitled Columbia Crew Survival Investigation Report, produced by a second commission, the Spacecraft Crew Survival Integrated Investigation Team (SCSIIT). NASA had commissioned this group, "to perform a comprehensive analysis of the accident, focusing on factors and events affecting crew survival, and to develop recommendations for improving crew survival for all future human space flight vehicles."^[30] The report concluded that: "The Columbia depressurization event occurred so rapidly that the crew members were incapacitated within seconds, before they could configure the suit for full protection from loss of cabin pressure. Although circulatory systems functioned for a brief time, the effects of the depressurization were severe enough that the crew could not have regained consciousness. This event was lethal to the crew." The report also concluded: * The crew did not have time to prepare themselves. Some crew members were not wearing their safety gloves, and one crew member was not wearing a helmet. New policies now give the crew more time to prepare for descent. * The crew's safety harnesses malfunctioned during the violent descent. The harnesses on the three remaining shuttles have since been upgraded. The key recommendations of the report included that future spacecraft crew survival systems should not rely on manual activation to protect the crew.^[31] [edit ] Possible emergency procedures Hypothetical rescue scenario with /Atlantis / below /Columbia/^[32] Hypothesized rescue EVA^[32] The CAIB determined a rescue mission, though risky, might have been possible provided NASA management took action soon enough.^[32] ^[33] The CAIB determined that had NASA management acted in time, two possible contingency procedures were available: a rescue mission by shuttle /Atlantis /, and an emergency spacewalk to attempt repairs to the left wing thermal protection. Normally a rescue mission is not possible, due to the time required to prepare a shuttle for launch, and the limited consumables (power, water, air) of an orbiting shuttle. However, /Atlantis/ was well along in processing for a March 1 launch on STS-114 , and /Columbia/ carried an unusually large quantity of consumables due to an Extended Duration Orbiter package. The CAIB determined that this would have allowed /Columbia/ to stay in orbit until flight day 30 (February 15). NASA investigators determined that /Atlantis/ processing could have been expedited with no skipped safety checks for a February 10 launch. Hence if nothing went wrong there was a five-day overlap for a possible rescue. As mission control could deorbit a shuttle but could not control the orbiter's reentry and landing, it would likely have sent /Columbia/ into the Pacific Ocean;^[32] NASA has since developed the Remote Control Orbiter system to permit mission control to land a shuttle. NASA investigators determined on-orbit repair by the shuttle astronauts was possible but risky, primarily due to the uncertain resiliency of the repair using available materials.^[32] ^[33] /Columbia/ did not carry the Canadarm , or Remote Manipulator System, which would normally be used for camera inspection or transporting a spacewalking astronaut to the wing. Therefore an unusual emergency EVA would have been required. While there was no astronaut EVA training for maneuvering to the wing, astronauts are always prepared for a similarly difficult emergency EVA to close the external tank umbilical doors located on the orbiter underside, which is necessary for reentry. Similar methods could have reached the shuttle left wing for inspection or repair.^[32] For the repair, the CAIB determined the astronauts would have to use tools and small pieces of titanium, or other metal, scavenged from the crew cabin. These metals would help protect the wing structure and would be held in place during re-entry by a water-filled bag that had turned into ice in the cold of space. The ice and metal would help restore wing leading edge geometry, preventing a turbulent airflow over the wing and therefore keeping heating and burn-through levels low enough for the crew to survive re-entry and bail out before landing. Because the NASA team could not verify that the repairs would survive even a modified re-entry, the rescue option had a considerably higher chance of bringing /Columbia/'s crew back alive.^[32] [edit ] Sociocultural aftermath [edit ] Fears of terrorism Despite some initial fears^[/citation needed /] after announcement in the news that Columbia suffered an explosion over Palestine, Texas and that the addition of the first Israeli astronaut to the crew had made the /Columbia/ a more likely target for terrorists, there is no evidence to support any theory that terrorism was involved. In any case, security surrounding the launch and landing of the space shuttle had been increased to ward off any potential terrorist attack.^[34] The Merritt Island launch facility, like all sensitive government areas, had increased security measures put in place in the wake of the September 11 attack . Gordon Johndroe, spokesman for the United States Department of Homeland Security , stated: "There is no information at this time that this was a terrorist incident." [edit ] Purple streak image The /San Francisco Chronicle / reported that an amateur astronomer had taken a five-second exposure that appeared to show "a purplish line near the shuttle" during re-entry.^[35] The CAIB report concluded that image was the result of "camera vibrations during a long-exposure".^[36] [edit ] Film hoax In a hoax inspired by the destruction of /Columbia/, some images that were purported to be satellite photographs of the shuttle's explosion turned out to be screen captures from the opening scene of the 1998 science fiction film /Armageddon /, where the shuttle /Atlantis/ is destroyed by asteroid fragments.^[37] In reality, /Columbia/ disintegrated rather than exploded. In response to the disaster, FX pulled /Armageddon/ from that night's schedule, replacing it with /Aliens /.^[38] [edit ] Memorials Search Wikinews Wikinews has related news: /*NASA holds ceremony to commemorate anniversary of Space Shuttle Columbia disaster */ On February 4, 2003, President George W. Bush and his wife Laura led a memorial service for the astronauts' families at the Lyndon B. Johnson Space Center . Two days later, Vice President Dick Cheney and his wife Lynne led official Washington and the rest of the nation in paying tribute at a similar service at Washington National Cathedral . During that service, singer Patti LaBelle sang "Way up There".^[39] /Columbia/ Memorial in Arlington National Cemetery /Columbia/ Memorial on Mars On March 26 the United States House of Representatives ' Science Committee approved funds for the construction of a memorial at Arlington National Cemetery for the STS-107 crew. A similar memorial was built at the cemetery for the last crew of /Challenger/ . On October 28, 2003, the names of the astronauts were added to the Space Mirror Memorial at the Kennedy Space Center Visitor Complex . The Houston Astros , who reside in the same city as Johnson Space Center and whose team name honors the U.S. space program, honored the crew on April 1, 2003, the Opening Day of the season, by having seven simultaneous first pitches thrown by family and friends of the /Columbia/ crew. For the National Anthem , 107 NASA personnel, including flight controllers and others involved in /Columbia’s/ final mission, carried a U.S. flag onto the field. In addition, the Astros wore the mission patch on their sleeves and replaced all dugout advertising with the mission patch logo for the entire season.^[40] In 2004, President Bush conferred posthumous Congressional Space Medals of Honor to all 14 astronauts lost in the /Challenger/ and /Columbia/ accidents. NASA named several places in honor of /Columbia/ and her crew. Seven asteroids discovered in July 2001 at the Mount Palomar observatory were officially given the names of the seven astronauts: 51823 Rickhusband , 51824 Mikeanderson , 51825 Davidbrown , 51826 Kalpanachawla , 51827 Laurelclark , 51828 Ilanramon , 51829 Williemccool .^[41] On Mars , the landing site of the rover /Spirit / was named /Columbia/ Memorial Station, and included a memorial plaque to the /Columbia/ crew mounted on the back of its high gain antenna. A complex of seven hills east of the /Spirit/ landing site was dubbed the Columbia Hills ; each of the seven hills was individually named for a member of the crew, and Husband Hill in particular was ascended and explored by the rover. Back on Earth, NASA's National Scientific Balloon Facility was renamed the Columbia Scientific Balloon Facility . Other tributes included the decision by Amarillo, Texas , to rename its airport Rick Husband Amarillo International Airport , after its native son and commander of STS-107. State Route 904 was renamed Lt. Michael P. Anderson Memorial Highway, as it runs through Cheney, Washington - the town where he graduated from high school. A mountain peak near Kit Carson Peak and Challenger Point in the Sangre de Cristo Range was renamed Columbia Point , and a dedication plaque was placed on the point in August 2003. Seven dormitories were named in honor of /Columbia/ crew members at the Florida Institute of Technology , Creighton University , The University of Texas at Arlington , and the Columbia Elementary school in the Brevard County School District . The Huntsville City Schools in Huntsville, Alabama , a city strongly associated with NASA, named their most recent high school Columbia High School as a memorial to the crew. A Department of Defense school in Guam was re-named Commander William C. McCool Elementary School.^[42] The City of Palmdale , the birthplace of the entire shuttle fleet, renamed a major thoroughfare /Avenue M/ to /Columbia Way/ after the disaster in honor of the lost shuttle and its crew. In October, 2004, both houses of Congress passed a resolution authored by US Representative Lucille Roybal-Allard and co-sponsored by the entire contingent of California representatives to Congress, naming Downey California’s Space Science Learning Center the Columbia Memorial Space Science Learning Center (CMSSLC is located at the former manufacturing site of the space shuttles, including the Columbia and the Challenger). The US Air Force 's Squadron Officer School at Maxwell Air Force Base , Alabama renamed their auditorium in Colonel Husband's honor. He was a distinguished graduate from the program. NASA later named a supercomputer "Columbia" in the crew's honor. A U.S. Navy compound at a major coalition military base in Afghanistan is named Camp McCool in honor of Pilot William C. McCool. In addition, the athletic field at Coronado High School in Lubbock, Texas , was re-named the "Willie McCool Track and Field" in his honor; McCool was a Coronado graduate. A proposed reservoir in Cherokee County in Eastern Texas is to be named Lake Columbia.^[43] On February 5, 2003 the space agency of India, ISRO , renamed one of its meteorological satellites METSAT as Kalpana-1 in memory of the Indian-born American astronaut Kalpana Chawla. [edit ] Impact on space programs Following the loss of /Columbia/, the space shuttle program was suspended. The further construction of the International Space Station was also delayed, as the space shuttles were the only available delivery vehicle for station modules. The station was supplied using Russian unmanned /Progress / ships, and crews were exchanged using Russian-manned /Soyuz/ spacecraft , and forced to operate on a skeleton crew of two. In late July 2003, an Associated Press poll revealed that Americans' support for the space program remained strong. Two-thirds believed the space shuttle should continue to fly and nearly three-quarters said that the space program was a good investment. On the question of sending humans to Mars , 49% thought it was a good idea, while 42% opposed it. For sending civilians like teachers into space, 56% supported the idea and 38% opposed.^[/citation needed /] Less than a year after the accident, President Bush announced the Vision for Space Exploration , calling for the space shuttle fleet to continue flying to "fulfill our obligations to our international partners" by completing the International Space Station (ISS), with retirement by the year 2010 following the completion of the ISS, to be replaced by a newly developed Crew Exploration Vehicle for travel to lunar orbit and landing and to Mars. NASA planned to return the space shuttle to service around September 2004; that date was pushed back to July 2005. On July 26, 2005, at 10:39 a.m. EST, Space Shuttle /Discovery/ cleared the tower on the "Return to Flight" mission STS-114 , marking the shuttle's return to space. Overall the STS-114 flight was highly successful, but a similar piece of foam from a different portion of the tank was shed, although the debris did not strike the Orbiter. Due to this, NASA once again grounded the shuttles until the remaining problem was understood and a solution implemented. After delaying their re-entry by two days due to adverse weather conditions, Commander Eileen Collins and Pilot Jim Kelly returned /Discovery/ safely to Earth on August 9, 2005. Later that same month, the external tank construction site, Michoud Assembly Facility located in New Orleans, Louisiana was damaged by Hurricane Katrina , with all work shifts canceled up to September 26, 2005. At the time, there was concern that this would set back further Shuttle flights by at least two months and possibly more. The second "Return to Flight" mission, STS-121 , launched on July 4, 2006, at 2:37:55 PM (EDT), after two previous launches were scrubbed because of lingering thunderstorms and high winds around the launch pad. The launch took place despite objections from its chief engineer and safety head. This mission increased the ISS crew to three. A 5-inch (130 mm) crack in the foam insulation of the external tank gave cause for concern; however, the Mission Management Team gave the go for launch.^[44] Space Shuttle /Discovery/ touched down successfully on July 17, 2006 at 9:14:43 AM (EDT) on Runway 15 at the Kennedy Space Center . On August 13, 2006, NASA announced STS-121 had shed more foam than they expected. While this did not delay the launch for the next mission, STS-115 , originally set to lift off on August 27,^[45] the weather and other technical glitches did, with a lightning strike, Hurricane Ernesto and a faulty fuel tank sensor combining to delay the launch until September 9. On September 19, landing was delayed an extra day to examine /Atlantis/ after objects were found floating near the shuttle in the same orbit. When no damage was detected, /Atlantis/ landed successfully on September 21. The /Columbia/ Crew Survival Investigation Report released by NASA on December 30, 2008 made further recommendations to improve a crew's survival chances on future space vehicles, such as the Orion moon program. These include improvements in crew restraints, finding ways to deal more effectively with catastrophic cabin depressurization, more "graceful degradation" of vehicles during a disaster so crews will have a better chance at survival, and automated parachute systems.^[30] [edit ] See also Flag of Texas.svg /*Texas portal */ * Apollo 1 * Space Shuttle Challenger disaster * Expedition 6 [edit ] References 1. *^ * "Columbia's Problems Began on Left Wing" . Space.com. http://www.space.com/missionlaunches/sts107_leftwing_030201.html. Retrieved February 26, 2008. 2. *^ * Columbia Accident Investigation Board (August 2003). "6.1 A History of Foam Anomalies (page 121)" (PDF). http://caib.nasa.gov/news/report/pdf/vol1/chapters/chapter6.pdf. Retrieved 2007-08-03. 3. *^ * "Molten Aluminum found on Columbia's thermal tiles" . /USA Today/. Associated Press. March 4, 2003. http://www.usatoday.com/news/nation/2003-03-04-shuttle-investigation_x.htm. Retrieved August 13, 2007. 4. *^ * Century of Flight. "The Columbia space shuttle accident" . http://www.century-of-flight.net/Aviation%20history/space/Columbia%20accident.htm. Retrieved August 13, 2007. 5. ^ ^/*a*/ ^/*b*/ William Harwood (March 27, 2009). "Legendary commander tells story of shuttle's close call" . Spaceflight Now. http://www.spaceflightnow.com/shuttle/sts119/090327sts27/. Written for CBS news /Space Place/. 6. *^ * Columbia Accident Investigation Board (August 2003). "6.1 A History of Foam Anomalies (PDF)" (PDF). http://caib.nasa.gov/news/report/pdf/vol1/chapters/chapter6.pdf. Retrieved 2007-08-03. 7. *^ * Columbia Accident Investigation Board (2003). "CAIB Recommendation R6.3-2 (PDF)" (PDF). http://caib.nasa.gov/news/report/pdf/vol1/chapters/chapter5.pdf. Retrieved January 30, 2006. 8. *^ * Columbia Accident Investigation Board, (2003) Volume 1, Chapter 6, p. 138.Chapter 6 (pdf). Retrieved June 8, 2006. 9. *^ * "nasa-global.speedera.net" (PDF). http://anon.nasa-global.speedera.net/anon.nasa-global/CAIB/CAIB_lowres_full.pdf. Retrieved 2007-07-27. 10. ^ ^/*a*/ ^/*b*/ Columbia Accident Investigation Board (2008). "Columbia Crew Survival Investigation Report" . http://www.nasa.gov/pdf/298870main_SP-2008-565.pdf. 11. *^ * Columbia Accident Investigation Board (2003). "Report of Columbia Accident Investigation Board, Volume I" . http://www.nasa.gov/columbia/home/CAIB_Vol1.html. Retrieved January 4, 2006. 12. *^ * Bush, George W. (2003). "President Addresses Nation on Space Shuttle Columbia Tragedy" . The White House. http://georgewbush-whitehouse.archives.gov/news/releases/2003/02/20030201-2.html. Retrieved January 4, 2006. 13. *^ * "In Search Of..." . http://researchernews.larc.nasa.gov/archives/2003/050903/Search.html. Retrieved 2009-02-09. 14. *^ * awextra@arrl.org (2003). "/Hams Aid Columbia Debris Search in Western States/" . American Radio Relay League, Inc.. http://www.arrl.org/news/stories/2003/02/26/2/?nc=1. Retrieved 2007-02-01. 15. *^ * Szewczyk, Nathaniel, et al. (2005). "/Caenorhabditis elegans/ Survives Atmospheric Breakup of STS-107, Space Shuttle Columbia" . Mary Ann Liebert, Astrobiology. http://www.liebertpub.com/prdetails.aspx?pr_id=428. Retrieved November 2, 2006. 16. *^ * "Worms survived Columbia disaster" . BBC News. 2003-05-01. http://news.bbc.co.uk/2/hi/science/nature/2992123.stm. Retrieved 2005-12-16. 17. *^ * Worms Survive Shuttle Disaster Fall 2003 18. *^ * "The 'Columbia' Debris Recovery Helo Crash" . Check-Six.com. http://www.check-six.com/Crash_Sites/STS107-N175PA.htm. Retrieved 2009-09-01. 19. *^ * "Shuttle debris offered online" . BBC News. 2003-02-03. http://news.bbc.co.uk/2/hi/technology/2720225.stm. Retrieved 2007-05-27. 20. *^ * "Debris Amnesty Ends, 9 May Face Looting Charges" . Associated Press. 2003-02-08. http://www.space.com/missionlaunches/sts107_amnesty_030208.html. Retrieved 2009-06-22. 21. *^ * "Divers Find Shuttle's Front Landing Gear" . Fox News. 2003-02-19. http://www.foxnews.com/story/0,2933,78993,00.html. Retrieved 2010-04-25. 22. *^ * "NASA begins packing up shuttle debris for storage" . USA Today. 2003-09-10. http://www.usatoday.com/news/nation/2003-09-10-space-shuttle-storage_x.htm. Retrieved 2009-06-22. 23. *^ * Fonseca, Brian (2008-05-07). "Shuttle Columbia's hard drive data recovered from crash site" . Computerworld.com. http://www.computerworld.com/action/article.do?command=viewArticleBasic&articleId=9083718. Retrieved 2009-09-01. 24. *^ * "The Physics of Whipped Cream" . Science.nasa.gov. http://science.nasa.gov/headlines/y2008/25apr_cvx2.htm. Retrieved 2009-09-01. 25. *^ * Dittemore, Ron (2003). "CNN Breaking News - NASA Briefing, Part I" . CNN. http://transcripts.cnn.com/TRANSCRIPTS/0302/01/bn.05.html. Retrieved January 4, 2006. 26. *^ * Woods, David (2004). "Creating Foresight: Lessons for Enhancing Resilience from Columbia" (PDF). http://csel.eng.ohio-state.edu/woods/space/Create%20foresight%20Col-draft.pdf. Retrieved February 1, 2005. 27. *^ * Sparks, Scotty (2003). "Water Absorption by Foam" (PDF). NASA. http://www.nasa.gov/columbia/caib/PDFS/VOL4/F01.PDF. Retrieved August 9, 2006. 28. *^ * Justin Kerr (2003). "Impact Testing of the Orbiter Thermal Protection System (PDF)" (PDF). http://research.jsc.nasa.gov/PDF/Eng-20.pdf. Retrieved January 30, 2006. 29. *^ * Columbia Accident Investigation Board (2003). "Report of Columbia Accident Investigation Board, Volume I, chapter 3, page 78 (PDF)" (PDF). http://www.globalsecurity.org/space/library/report/2003/caib-report_vol1_chapter3.pdf. Retrieved January 4, 2006. 30. ^ ^/*a*/ ^/*b*/ "Layout 1" (PDF). http://www.nasa.gov/pdf/298870main_SP-2008-565.pdf. Retrieved 2009-09-01. 31. *^ * Columbia Crew Survival Investigation Report . 32. ^ ^/*a*/ ^/*b*/ ^/*c*/ ^/*d*/ ^/*e*/ ^/*f*/ ^/*g*/ Columbia Accident Investigation Board (2003). "In-Flight Options Assessment, Volume II, appendix D.12 (PDF)" . http://www.nasa.gov/columbia/caib/PDFS/VOL2/D13.PDF. Retrieved January 30, 2006. 33. ^ ^/*a*/ ^/*b*/ Columbia Accident Investigation Board (2003). "Report of Columbia Accident Investigation Board, Volume I, chapter 6, page 173 (PDF)" (PDF). http://anon.nasa-global.speedera.net/anon.nasa-global/CAIB/CAIB_lowres_chapter6.pdf. Retrieved January 4, 2006. 34. *^ * "Israel mourns first astronaut's death" . CNN. 2003-02-01. http://www.cnn.com/2003/WORLD/meast/02/01/shuttle.israel.reax/. Retrieved 2004-02-24. 35. *^ * Russell, Sabin (2003-05-02). "Mysterious purple streak is shown hitting Columbia 7 minutes before it disintegrated" . sfgate.com. http://www.sfgate.com/cgi-bin/article.cgi?file=/c/a/2003/02/05/MN192153.DTL. Retrieved 2009-05-26. 36. *^ * Columbia Accident Investigation Board (2003). "Report of Columbia Accident Investigation Board, Volume III, Part 2, page 88 (PDF)" (PDF). http://caib.nasa.gov/news/report/pdf/vol3/part02.pdf. Retrieved August 18, 2006. 37. *^ * "Photos of the Shuttle Columbia Disaster? - BreakTheChain.org" . BreakTheChain.org